Pump... or Siphon?: Difference between revisions
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[[Category:Siphons]] | |||
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''' ''Message: [[Siphons]] Can Help Supply Water Needs in Lieu of Pumps'' ''' | |||
''Message: Siphons Can Help Supply Water Needs in Lieu of Pumps'' | |||
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During an effort to construct an upstream pad for a drill rig to perform investigation drilling along the outlet works of the dam, work crews ‐ inadvertently (and unknowingly) placed material over the outlet works. The blocked outlet works were not discovered until the reservoir was at full pool. It was impossible to make irrigation deliveries into the downstream canal. It was the beginning of the irrigation season and irrigators were not able to receive water. The irrigation project needed a solution that would deliver water during the entire irrigation season and not involve the high maintenance costs of renting pumps for a long duration. Calculations were performed and it was determined that a siphon was possible.</br> | During an effort to construct an upstream pad for a [[drill]] rig to perform investigation [[drilling]] along the outlet works of the dam, work crews ‐ inadvertently (and unknowingly) placed material over the outlet works. The blocked outlet works were not discovered until the reservoir was at full pool. It was impossible to make [[irrigation]] deliveries into the downstream canal. It was the beginning of the irrigation season and irrigators were not able to receive water. The irrigation project needed a solution that would deliver water during the entire irrigation season and not involve the high maintenance costs of renting pumps for a long duration. Calculations were performed and it was determined that a siphon was possible.</br> | ||
Take-aways from the project: | Take-aways from the project: | ||
#The dam crest was notched to reduce the lift height of the siphon. | #The dam crest was notched to reduce the lift height of the siphon. | ||
#The bending radius of the HDPE pipe was used to elimiate bend fittings. | #The bending radius of the HDPE pipe was used to elimiate bend fittings. | ||
#Three 18-inch siphons were installed. | #Three 18-inch siphons were installed. | ||
#Construction time was 5 days. | #[[Construction]] time was 5 days. | ||
#Steel bands were placed around the inlet side of the pipe to counter buoyancy of the pipe. | #Steel bands were placed around the inlet side of the pipe to counter buoyancy of the pipe. | ||
#The maximum flow rate was 60 cfs. | #The maximum flow rate was 60 cfs. | ||
#Vortices formed when the siphon lift was approximately 16 feet. Valves were throttled back and the vortices subsided. | #Vortices formed when the siphon lift was approximately 16 feet. Valves were throttled back and the vortices subsided. | ||
From Guidelines for Use of Pumps and Siphons for Emergency Reservoir Drawdown, Morrison Maierle, Inc. 2012 | From Guidelines for Use of Pumps and Siphons for Emergency [[Reservoir Drawdown]], Morrison Maierle, Inc. 2012 | ||
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Latest revision as of 03:18, 2 December 2022
Message: Siphons Can Help Supply Water Needs in Lieu of Pumps
During an effort to construct an upstream pad for a drill rig to perform investigation drilling along the outlet works of the dam, work crews ‐ inadvertently (and unknowingly) placed material over the outlet works. The blocked outlet works were not discovered until the reservoir was at full pool. It was impossible to make irrigation deliveries into the downstream canal. It was the beginning of the irrigation season and irrigators were not able to receive water. The irrigation project needed a solution that would deliver water during the entire irrigation season and not involve the high maintenance costs of renting pumps for a long duration. Calculations were performed and it was determined that a siphon was possible.
Take-aways from the project:
- The dam crest was notched to reduce the lift height of the siphon.
- The bending radius of the HDPE pipe was used to elimiate bend fittings.
- Three 18-inch siphons were installed.
- Construction time was 5 days.
- Steel bands were placed around the inlet side of the pipe to counter buoyancy of the pipe.
- The maximum flow rate was 60 cfs.
- Vortices formed when the siphon lift was approximately 16 feet. Valves were throttled back and the vortices subsided.
From Guidelines for Use of Pumps and Siphons for Emergency Reservoir Drawdown, Morrison Maierle, Inc. 2012
Note: The content on this page was originally created as part of DamOutletWorks.org (DOWL, 2018). It has subsequently been updated and reformatted as part of the Dam Safety Toolbox.
Revision ID: 4746
Revision Date: 12/02/2022